Friday, November 25, 2016

A Few New Things...


It seemed like a good idea at the time

So, it with winter coming I decided that I would get a few things done while the weather was still warm enough to work.  I had not been riding too much and finally I had a chance to take care of a few things.  Since the rebuild of the carbs, I noticed that I was not getting quite the high-end performance I had expected with a nagging miss around 3000rpm.

Fix the obvious

Points and condenser

I started by replacing the points and condenser.  Not a bad idea.  The old ones were so shot I could see them arc across the points themselves to the arm that holds the points.  Hey, that may have been the miss.  Or not.   It certainly helped and thanks to the magic points adjustment tool ($24 well spent) I went for keeping with mechanical timing.  I guess I just like the thought as opposed to an electronic system that just flat dies by the road with absolutely no options.  Still not satisfied I tried to balance the carbs with my home made an manometer.  What is that?


Detour: The manometer from hell..for $6

To measure your vacuum on the carbs and balance them you can spend a lot and get a fancy set of gauge that giggle and bounce making it really hard to see if things are steady.  That costs around $60.  Or you can spend $6 and get a more accurate gauge.   Attach a 4 foot length of 1x2 perpendicular between a couple 3ft lengths of 2x4 so it sticks up in the air and the base is stable enough so it does not fall over.  buy 10 ft of 1/4 in clear plastic aquarium hose. and loop it from the top of the 1x2 back up to the top.  secure it gently with zip ties.  Fill it with some automatic tranny fluid so you have about a foot in each column of tubing.  Secure the top.  You might have to use a couple short lengths of fuel line to keep the upper ends of the tubing from kinking as you bring them down to the bike.  now when the bike runs, the carb drawing the most vacuum will pull some of that ATF up its side of the loop.  Instead of trying to read a little bouncing dial you have a nice stable column of fluid that probably moves one inch for every 1/32 inch giggle on a needle.  It is really precise.  Pure physics.

Fuel flow...or not.

So, again, that helped but not cured.  Time to check fuel flow because it seemed as though one carb might be starving.  Pulled the petcocks and found them to be in poor shape.  Replaced one outright ($45) when dumbo broke it while tightening it.  I will not tell that story. Ever.  New screens, one new petcock...what could be a better time to look a the tank.

Tank sealing 101

I looked in the tank and realized that years ago someone had sealed it and that seal was shot.  Gross junk.  So, here's what I did.

  • Get a jar of naval jelly ($6) 
  • Gallon of acetone ($10)
  • Box of baking soda.  Don't use your spouse's from the kitchen.  Get you own. (Tip for a 35yr marriage #43)
  • An 8oz can of POR-15 49216 tank sealer ($13)
  •  a short length 18in or so of brass chain.  small stuff, that figure 8 type.
  • 2 rubber stoppers that fit the petcocks...BAD MEMORY..I thing they are 1/2 inch or so.  Measure yourself. ($3) 
  • A "pick up tool"
  • Air Compressor
  • Hair Dryer or Shop Vac 
  • Enough protective gear for a chemical attack.
  • A couple dark nights with no neighbors around.


Flush the tank with water.  Add the chain and shake that tank with water to bust up all the loose old sealer and rust.  Repeat until dawn or the only thing left in the tank is whatever sealer is still sticking.  
Add the acetone and put the gas cap on.  shake it every few hours for a day or so.  The old sealer is turning into sludge.   Drain that mess back into the Acetone can and Flush the tank with water.  If convinced its all out of there, pull out the chain.

Now, add the Naval Jelly and warm water.  Half tank. slosh it to break up the jelly.  This is galvanizing the metal with an acid.  fill it to the top and let is set for a day.   Drain it, flush and fill with water and baking soda.  Now the acid is neutralized, and your driveway is the cleanest it has been in years.

Drain it, flush it with water like crazy and blow it out with Compressed Air.  Dry with hairdryer or shop vac blowing into the tank.

Follow directions on POR-15.  You've already cleaned and prepped the tank just dandy.  The directions are shake it, pour it. tape off the opening for the gas cap and start methodically turning tand tilting that tank.  The BMW has a 6 gallon tank and you are going to get about 2-3 oz of extra sealer when you drain it finally.  It is a thin, thin coat.  Let that sucker dry for 96 hours or whatever.  Don't rush it.  So for $35 it is clean, galvanized and then sealed with aluminum powder suspended in a fuel proof paint.  Yipee, it will last forever and so much nicer that that gooey plastic sealer that was in there before.  Yellow mung.

Back to the Petcocks and some other thoughts.

Reinstalled the screens and petcocks plus...a new set of in-line filters ($10) and have great fuel flow.  Still a little missy, so time to re-check floats.  I think they were a little low and might have given it some fuel starvation?  Anyway, it seems better.  Time to do some other checks or just have a pro play with it for an hour and get it right.  I'm pretty happy with the valve clearances and associated noise.  Its been a few years since I checked them - so it might be time before I spend money on a real mechanic.  Something I can do and feel good doing.

Starter problem - not so fast!  It's the cable, stupid.

So I was doing some checks, balancing the carbs by letting them carry the idle individually until they would just die after a few kicks.  Really using the starter a lot.  All of a sudden, I got the chattering sound of the bendix not fully engaging the flywheel to the point where the sucker would get full voltage and turn!..and its not the first time.  A few weeks ago, I changed out my old Bosch for a Chinese knockoff Valeo.  Yeah, I know.  But it was doing this same thing.  Chattering.  It stopped when I put it all back together and the new starter seems okay.  Now its a few weeks later and its doing it again!  Then I hear it.  POP...   I spotted a freaking spark off my negative ground cable!  Until I moved it around I had no idea it had rotted and broken by one of the connectors.  Probably 1/3 of the wire gone.  Well.  Replaced the ground wire and it starts like a champ.  Obviously that old Bosch was not the problem and now I have a spare starter handy for the day the former democracy demonstrators turned laborers at Tienanmen Industries Starter Factory #7 located near an old above ground nuke test site in the Western Deserts fails me.  What do those people want?  A 12 hour day and  a 6 day week?

So that's almost the end of the story


Thursday, August 20, 2015

32mm or 40mm Jet Needle


You may find yourself in this position - I did.   I'm rebuilding my 32mm bing carbs and having ordered a new set of jet needles I noticed that they were a little bit shorter than what was installed.

It turns out there was a simple shipping error from a very reputable and super company who I called and immediately set about to get me fixed.

In the process of researching however, I noted a lack of simple information about these needles.

Length of Main Jet Needle

Pre 05/1983 Bing 32mm is 61mm long

40mm is 55mm long

For what it's worth.

Friday, November 18, 2011

Still Strong.

I really haven't been the greatest blogger on this the last few years. I think as a result a lot of things going on in the real world and in my own world. But I wanted to bring you up to date on what's going on the old BMW. She still running strong and riding great.Despite having over 98,000 miles on her she still turns heads and gets people waving and I hope a few people envious. Considering how little I spent  I have had such joy writing that motorcycle is I cannot express.

Going to begin to summarize in a few blogs saw the work of those happen to the bike last few years and I'll do my best to get some pictures up on the web also.

Removing the Luggage Racks

In an effort to clean up the bikes lines, I removed the luggage racks. I really have not been using them and they just  continued kind of mess up the lines of motorcycle.

Wednesday, January 30, 2008

Repairing the Kill Switch Lever

When I bought the bike the kill switch was functioning but very...very sensitive. As well the end of the plastic thumb lever was broken off. Initially I rebuilt the broken piece using a plastic epoxy putty. The switch had become finicky and rather than experience one of those embarrassing and dangerous "surprise engine kills" while going down the road and inadvertently touching the kill switch with a winter glove while adjusting the mirror stalk -does it sound like this may have happened to me? - I took the switch apart and did some maintenance to it. I'll blog that separately. So, the plastic thumb part was weakened as I attempted to trouble shoot the switch. I cut a trough into the back side of the switch and fitted in a piece of 6d finishing nail.


Covered it up with epoxy and Viola...good for another 30 years.

Sunday, January 27, 2008

Installing the Thunderchild Voltage Regulator and Diode Board



My voltage regulator and diode board arrived. Also included were the little studs to mount the board to the engine case. Big improvement over the 30year old rubber ones. One was all but gone, another cracked through and the diode board was holding on for dear life by two rubber mounts and one of the grounding wires was about cut through from apparently being pinched by the case during a reassembly some time ago. See pic













Note that the old board was in 'pretty good' shape considering this is the original board, not the upgraded one done a couple of years later. Those are identified by a gray stripe across them.










It is VERY tight in the back of the case to get these studs in place. But Thunderchild has made a great work around. The bold shaft is cut for a metric Allen key..about a 4 mm. Bend one of your old keys at a 45 degree angle to be able to place it under the starter on the lower right stud.

Thread your washer and nut OVER the Allen key.

Place the stud through the case and then place the allen key in the stud allen key hole. Picture shows how the key with the nut and washer is placed in the allen key hole.

This allows you to BEGIN threading the washer and nut. DO NOT thread completely. Just get it started and pull out the Allen key. If you don't you end up with the allen key jammed against the starter. Just use is as a temproary holder so you don't drop the washer or nut.


Here is the allen key on the right Upper nut. The Right Lower is the hard to reach one.













Finally, placed a little hose material behind the voltage regulator as padding. What the heck.

Installing the Front Tire - Brake Checks


Installed the front tire and did brake adjustments. While the tire and wheel were off at ADVENTURE BMW in Chesapeake Virginia, I took the time to do some preservation work on the forks and brake calipers.

2008 January Maintenance Log

Last Log Mileage: 95500(est)

Current Mileage: 94707

Monthly Total: 207

Total Miles Owned (since 94272) 1435

01 JAN 08 - Happy New Year! Lots planned this month to get the bike ready for Spring

Saturday, January 5, 2008

Haste Makes Waste


I finally got things back together and have the headlight in the shell using my own approach. The headlight is a standard Halogen Sylvannia light for a car. It still has the ring from the fairing attached to it, but this is not going to work with the standard shell....what to do?

The ring fits inside the shell, but there is some space around it. Here's my idea. I bought some felt weatherstripping and placed a length of it around the outside of the headlight shell and secured it with electrical tape. that extended the edge of the shell with a flexible, soft felt ring. I did the same for the headlight and magically the two rings of felt nest inside each other "pretty good". I then wrapped the joint in more tape. Looks great, works fine.

Only problem was that when I was doing all this, I did not disconnect the headlight from its connector. I did not know it but one of the connections was pulled out and I did not know I did not have a headlight until I was all suited up and ready to ride this morning (30 F).

Well, I fixed it enough for the ride and bought a new $2.50 connector at PEP Boys. Another little project for another time.

Friday, January 4, 2008

Troubleshooting the Flasher Relay

Reference: Troubleshoot Turn Signal Relay - Turn Signal works, indicator flashes once and turns off. Hella DOT TBB 26 1-4x21W-12V 4DB 002 479-08 (A)71315 See Standard Troubleshooting Disclaimer on Main Page


Odd thing. I finally think I had one of those experiences we were told we would someday have. It was like the scene in Red Planet when Val Kilmer says (trying to figure out their way to the Mars Habitat Shelter before their air runs out) :"This is it. That moment our teachers said that someday algebra would save our lives". I now know a bit more about the flasher relay than I would like and I think physics saved me $59.

Removing the fairing was pretty simple actually. As to the turn signals, they used to be up on the fairing and had two wires each - a hot and a ground. The ground went back to the 31 block (the brown one on the bottom - brown as ground). So when the light was on its circuit was fairly clean although connectors can create some resistance. Lets just consider this the 'normal state' of that circuit.

How does a turn signal work? There are several good sites - check out the Vespa repair site. It has a fine explanation.


Basically for this troubleshooting you need to know that there are two magnetic coils in the relay that serve to interrupt the circuit. One is associated with the lights and one acts in parallel and runs the little turn signal indicator light in the instrument console.

When I went to the stalk lights I increased the resistance on the circuit since they are now grounded through the frame and not the block. This affected the behavior of the capacitor in the relay. It apparently had enough juice to pull down its own coil repeatedly, but after the first discharge it failed to provide adequate amps to the second coil (indicator on instrument cluster) to allow it to repeat. So when you turn on the signal it works, but the indicator blinks once and then does not blink again.

I opened up the relay by spreading the base of the cap and examined the relay. Be VERY GENTLE. These things can bounce around all day, but there are some very fine parts that if touched roughly can damage the entire piece. After a couple of days learning about relays and looking at this problem I did the scientific thing of...(See Standard Disclaimer)...placing my fingernail behind the bar that completes the signal and push it about 1/64th of an inch closer to its coil. Bingo! It started to work just fine. So I could either 1) adjust the rest for this bar and bend it closer and reduce the travel distance...or 2) adjust the spring tension and and make it easier to move the bar. I did 2) since it looked like the spring was designed to have its tension adjusted. That's it... a $59 replacement avoided. Clean it up with electronic parts cleaner, grease it with some dielectric grease to preserve and clip it back into the bike. Good riding!

Sunday, December 30, 2007

Wiring Chart for R100/7

I have finally removed the Vanguard fairing from the bike. It is a period piece made in England and frankly looks pretty good, all considered.


So in the process of removing it I made some notes on the wiring . Below is a chart explaining how the wiring harness was connected for the fairing. The middle image is a view of the wiring harness half that was connected to the bike's connector block in the headlight. It shows the connectors and the wiring color codes of the harness wires. On the right is the mirror image of the fairing connector, the female end that is attached to the fairing. It is a mirror image of the male end naturally. The fairing only has a few connections:
  1. Common to the light relay - acts as ground for light circuit (connector 2)
  2. High Beam (connector 1)
  3. Low Beam (connector 3)
  4. Turn signals (connector 5 Right and 8 Left)
  5. and a ground for the turn signals (connector 4)ow beam as well as the turn signals which need ground.
Finally, on the left is where the wiring harness on the bike side connects to the appropriate circuits on the wiring block in the headlight. These are color coded and also are associated with specific circuits.

So, the diagram below shows the headlight on the left (wiring block), male harness in the center (bike side) and female harness (fairing side) on the right.
The diagram below shows more detail and explains the wiring block in the headlight. If you read a wiring diagram in a Haynes manual, you understand the circuits, but that diagram is not "real world 100%. This diagram shows you what that connector block in the headlight looks like, what circuits are attached to what set of connections and finally where do I connect those wires from the bike side male wiring harness? That is easy, they are numbered as well as color coded.

Note that some of these blocks have unused terminals. They are shown as white. Now there is a white block....so I colored it off-white in this diagram.


The fairing headlight is a sealed beam auto type. Okay, I'll work with that and try to figure out how to mount it in the headlight shell.

Saturday, December 29, 2007

2007 December Maintenance Log

Must be the end of year..Santa is Here! Actually my wife. After much deliberation I realized it was time to face up to getting a new tire. Now I think I can ride over 30mph without white knuckles. I also ordered a Thunderchild diode board, mounting studs and fixed voltage regulator.

  • Pulled the front tire. (30min) Not too bad. Had to lightly drift out the axle as it was a long time since greasing. Dropped it off at Adventure BMW in Chesapeake, Virginia.
  • Removed fairing (2hrs) Only difficulty was documenting the wiring as I disconnected it and having to briefly disconnect the clutch cable. It had been routed inside of one of the fairing mounts.
  • Pulled the diode board

2007 November Maintenance Log

2007 October Maintenance Log

2007 September Maintenance Log

Squeaks and tweaks

Monday, September 3, 2007

03 SEP 07 Labor Day Weekend Mackay Is NWR NC

Last evening we attended a party in the neighborhood. They say that a promise made drunk is sacred. So it was that this morning 5 of us met for a ride. There was myself, Jim and his R850, Ian, Jim's neighbor and his H-D 1200, Todd and his "new" Honda VTX and the youngest member of the group, Adam and his Ninja. Pretty strange group, but short of Carson and his 919, that was every bike in our neighborhood.

30 AUG 07 95,000 Miles

First good milestone since owning.

2007 August Maintenance Log

Minor tweeks

2007 July Maintenance Log

July 15 Ordered and received a set of rockers and pushrods from an 81 RT. Funny though, I probably won't put them on. I spoke with the maintenance experts down at Adventure BMW in Chesapeake and was told that all I needed to do was to retorque the head and that the rocker assemblies 'float' on the head bolts. Sure enough...that made a big improvement.

Tuesday, June 12, 2007

2007 June Maintenance Log

Last Log Mileage: 94567



Current Mileage:


Cumulative Miles:0






01 JUNE 07 Did a very quick check on the valve clearances. Not much to do there since the noise seems to be coming from the end play in the rockers. Just a bother, not a problem. No performance issues related to rockers. Maybe in a few thousand miles.


10 JUNE 07 Brake Failure warning light coming on intermittently.


11 JUNE 07 Topped up brake fluid. Just a little low. Will have to monitor.


12 JUNE 07 Lost bid on Ebay for a set of rockers. Original gear, before the shim upgrade. Will have to continue to look. Perhaps I can snag a set of the newer ones from post 85. Had a nice test ride. Brakes are fine. Must keep on top of fluids.